News & View, Volume 44 | Failed Grade 91 “Soft” Pipe Bend - A Case Study Failure Occurred With Less Than 35,000 Operating Hours

News & Views, Volume 44 | Failed Grade 91 “Soft” Pipe Bend – A Case Study – Failure Occurred With Less Than 35,000 Operating Hours

By:  Kane Riggenbach and Tony Studer

News & View, Volume 44 | Failed Grade 91 “Soft” Pipe Bend - A Case Study Failure Occurred With Less Than 35,000 Operating HoursGrade 91 steel is widely used in tubes, headers and piping of superheaters and reheaters because of its higher strength at elevated temperature compared to low alloy steels such as Grade 22.  The improved strength is a result of a tempered martensitic microstructure with a fine distribution of carbonitride precipitates.  This microstructure is achieved through careful heat treatment: normalizing, tempering, and subsequent forming and post weld heat treatments.  If these heat treatments are not performed properly, then the strength of the material essentially reverts to that of a low alloy steel like Grade 22, and is usually accompanied by a reduction in hardness, leaving the Grade 91 material in a so-called “soft” condition.

This article summarizes a case study for Grade 91 material in the “soft” condition, which was responsible for a steam leak after only 5 years of operation, illustrating how this material condition can result in forced shutdowns and safety hazards.  It is because of these consequences that it is recommended to have a Grade 91 life management program to understand if your plant may have such vulnerability.

This case study provides general background to the steam leak and describes the subsequent metallurgical evaluations performed to verify that mal-heat treatment of the Grade 91 steel was the root cause of the leak.  A follow-on article (the next issue, Volume 45, of News and Views) will provide additional insight into local stresses and analytical prediction of such failures, as well as highlighting key aspects of a Grade 91 life management program.  Suffice it to say if this plant had implemented such a program, the vulnerability of the affected spool would have been identified and mitigating actions could have been taken to avoid the leak.

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News & View, Volume 43 | Metallurgical Lab- Dissimilar Metal Welds (DMW) in Boiler Tubing The need for confirmation- A Case Study

News & Views, Volume 43 | Metallurgical Lab: Dissimilar Metal Welds (DMW) in Boiler Tubing

By:  Tony Studer

The need for confirmation: A Case Study

News & View, Volume 43 | Metallurgical Lab- Dissimilar Metal Welds (DMW) in Boiler Tubing The need for confirmation- A Case StudyAs plants age, the need for inspection for service related damage to ensure unit reliability increases. There are several approaches that plants can take to reduce the risk of premature failures and proactively manage their DMWs. First is metallurgical sampling. Based on temperature profiles across the boiler, operating conditions, and operating history, DMWs can be selected for laboratory analysis. This will provide some insight into possible damage accumulation; however, the better approach, if damage is suspected, is to perform an ultrasonic inspection of the DMWs. This allows inspection of all the DMWs, and only requires access and surface preparation. If indications are detected, then tube sampling should be performed. It is critical to perform a metallurgical analysis of several of the DMWs suspected of containing service damage to confirm that the indications are service related and to help establish the extent of the damage compared to ultrasonic testing results. Typical DMW damage is described in the Featured Damage Mechanism article. The importance of the metallurgical analysis is demonstrated in the three following case studies.

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